Hello everyone, based on the results of this thread ( Previous Thread ), I've decided to make a more technical post about a problem I'm having with a broken mouse wheel shaft, what I've tried to repair it, and a new ideas about how to fix it. Hopefully a few of you have tried something like this before and have some insight, or just have some general feedback on my ideas to make the fix.
A Few Details:
*This is by far my favorite mouse ever.
*Mouse Model: Cooler Master Storm Recon [it has officially been discontinued]
*Unlike most wheels I've seen, this wheel is only 'flat' on one side (the 'click switch' side). The rotary switch side is actually concave because they use a circuit board extension with the small type LED light to get said light into the wheel. The design is quite clean, but it does make 'working' inside the wheel considerably difficult (and tolerances quite small).
*I personally don't exactly have a lot of tools/machinery available to me aside from scissors and hammers, so all my ideas are either what I could do personally or have 'exported' for some business to complete. That said, if you have some good idea that uses a reasonably easy to get tool, I'm all ears.
The Problem:
The shaft (on the rotary wheel side) cracked completely though, rendering the wheel unusable. See the damage here:
The fix that didn't really work out:
Basically I...
-tightly wrapped a half inch or so of paper around the broken shaft to use as a guide
-tried to place it flatly against the 'stub' of plastic inside the wheel (hard to tell by 'feel') since there isn't much there (the paper is left on since it is quite thin and sticks to the glue)
-take a bit of two part Gorilla glue and apply it to the guide shaft
-press the broken shaft down into the guide (taking care to align the 'jagged' bottoms as best as possible to minimize any length difference after the glue was added
-manually 'eyeball' whether or not the shaft was straight or not by looking at it and adjusting it with my finger, rotating it 90 degrees and doing the same
-let glue set for 24 hours
Result-> while this did appear to work, when the entire mouse shell was put back on the slight amount of wobble caused the wheel to grind against the sides of the mouse shell at certain positions, requiring a very hard 'click'. This hard click eventually caused the glue to give and I'm back where I started)
New Ideas:
1) Try the same 'fix' again
Pros: easy to do by myself, maybe I'll 'be better' at it this time?...
Cons: tolerance probably still won't be tight enough.
-probably my least favorite option.
2) Make a 3D model of the entire 'shaft part' and 3D print it using a clear-ish plastic or resin (and 'scuff it up' if the light is too bright).
Pros: should be accurate enough to fit more/less perfectly (not entirely sure what the tolerance on the 'rotary switch side' would need to be since it may require 6-16 slots to interface properly).
Cons: I'm really not sure how to remove the shaft 'nub' and other side of this thing...I'm not sure if it is pressure fit or glued into the larger wheel (or is actually one single piece and includes the wheel itself), but I don't think bashing it with a hammer would work.
-a great option -if- I could figure out how to remove the current shaft (otherwise I would probably need to make the entire wheel (not impossible, just more work).
3) Instead of using a floppy paper 'guide', make the guide out of 3D printed material.
Pros: simple to make.
Cons: even if it works, the glue may not be strong enough to hold. Not quite sure how to use the guide without it becoming stuck to the glue (or how to remove it without 'tilting' the shaft)...
-perhaps the most practical.
If anyone has tried something like this before / or just has some feedback on my ideas (perhaps you've done something generally related to them before) would be greatly appreciated.
A Few Details:
*This is by far my favorite mouse ever.
*Mouse Model: Cooler Master Storm Recon [it has officially been discontinued]
*Unlike most wheels I've seen, this wheel is only 'flat' on one side (the 'click switch' side). The rotary switch side is actually concave because they use a circuit board extension with the small type LED light to get said light into the wheel. The design is quite clean, but it does make 'working' inside the wheel considerably difficult (and tolerances quite small).
*I personally don't exactly have a lot of tools/machinery available to me aside from scissors and hammers, so all my ideas are either what I could do personally or have 'exported' for some business to complete. That said, if you have some good idea that uses a reasonably easy to get tool, I'm all ears.
The Problem:
The shaft (on the rotary wheel side) cracked completely though, rendering the wheel unusable. See the damage here:
![10xu595.jpg](/proxy.php?image=http%3A%2F%2Fi65.tinypic.com%2F10xu595.jpg&hash=120cbf160ab5721eee948462ec540834)
The fix that didn't really work out:
Basically I...
-tightly wrapped a half inch or so of paper around the broken shaft to use as a guide
-tried to place it flatly against the 'stub' of plastic inside the wheel (hard to tell by 'feel') since there isn't much there (the paper is left on since it is quite thin and sticks to the glue)
-take a bit of two part Gorilla glue and apply it to the guide shaft
-press the broken shaft down into the guide (taking care to align the 'jagged' bottoms as best as possible to minimize any length difference after the glue was added
-manually 'eyeball' whether or not the shaft was straight or not by looking at it and adjusting it with my finger, rotating it 90 degrees and doing the same
-let glue set for 24 hours
Result-> while this did appear to work, when the entire mouse shell was put back on the slight amount of wobble caused the wheel to grind against the sides of the mouse shell at certain positions, requiring a very hard 'click'. This hard click eventually caused the glue to give and I'm back where I started)
New Ideas:
1) Try the same 'fix' again
Pros: easy to do by myself, maybe I'll 'be better' at it this time?...
Cons: tolerance probably still won't be tight enough.
-probably my least favorite option.
2) Make a 3D model of the entire 'shaft part' and 3D print it using a clear-ish plastic or resin (and 'scuff it up' if the light is too bright).
Pros: should be accurate enough to fit more/less perfectly (not entirely sure what the tolerance on the 'rotary switch side' would need to be since it may require 6-16 slots to interface properly).
Cons: I'm really not sure how to remove the shaft 'nub' and other side of this thing...I'm not sure if it is pressure fit or glued into the larger wheel (or is actually one single piece and includes the wheel itself), but I don't think bashing it with a hammer would work.
-a great option -if- I could figure out how to remove the current shaft (otherwise I would probably need to make the entire wheel (not impossible, just more work).
![2exyb80.jpg](/proxy.php?image=http%3A%2F%2Fi67.tinypic.com%2F2exyb80.jpg&hash=615bcdd5276618b2a8ec03ec91a90583)
3) Instead of using a floppy paper 'guide', make the guide out of 3D printed material.
Pros: simple to make.
Cons: even if it works, the glue may not be strong enough to hold. Not quite sure how to use the guide without it becoming stuck to the glue (or how to remove it without 'tilting' the shaft)...
-perhaps the most practical.
If anyone has tried something like this before / or just has some feedback on my ideas (perhaps you've done something generally related to them before) would be greatly appreciated.